-Aerospace Engineering Student-
Screenshot 2020-09-12 215601.png

South West Rocketry

Sport Rocketry Team

 

South West Rocketry

The Early Years

 
 
2016 test launch

2016 test launch

Project Overview

Starting from the year 2013 I was a member of, and later led, a sport rocketry team to compete in the Team America Rocketry Challenge.

Every year my team was required to design a sport rocket to reach a target altitude and target flight duration while holding a raw hen’s egg on board. The rocket had to be at least 26” long and weigh no more than 650 grams at take-off. From 2016 onward I personally selected my teams and led them to the TARC National Competition maintaining six years of consecutively competing in the TARC national finals.


2017 DesIgn and flight performance

I designed the Rocket around the Cesaroni F-79 Motor in order to carry over the previews two years of flight data. After securing a sponsorship from Oxeon, who makes the Textreme line of carbon fiber fabrics, all major components were built with two layers of their 1017 fabric. I leveraged the use of 3D printing to construct much of the internal components, and used 0.125” aramid honeycomb to decrease weight in the fins.

The day before the TARC national competition, we suffered a rapid unscheduled disassembly of the main rocket due to cold weather deceasing the amount of friction on the main coupler. The backup rocket flew in the competition with less than optimal performance. At the end of everything we placed 65/700 in launch, third in presentation, and took home the “Most Innovative Approach to Mission“ award, presented by Raytheon.

Test Launch in Virginia

Test Launch in Virginia

IMG_20170425_191530.jpg

Altitude Control System: Spring Ejection

I designed our spring ejection system in Autodesk Fusion 360, and 3D printed its components from PLA. I designed the system to work as a “pusher” to separate the rocket and deploy the main parachute. This system was controlled by a miniaturized Arduino nano and a barometer. When the arduino red an altitude above the pre-determined threshold, it would spin a small DC motor that would disengage with a lead-screw allowing the spring to be released and the rocket to separate.

This system was incredibly reliable, and had no major impact on the barometric altimeter. This system was flight proven to control the rocket’s altitude to within +/- 15’.

Altitude Control System: CO2

In order to control when the parachute deploys on the rocket, I designed a system to accept a 1.5g 1100psi CO2 cartrage that would be pre-punctured and could be actuated by a small motor and an Arduino. With the oversight of a talented machinist, I milled the major components from 6061 Aluminum. In order to actuate the device, the motor would spin a lopsided drum (not shown) allowing a collar to slide down the barrel providing room for four ball bearings to move radially outwards, giving way for the CO2 cartridge to disengage the forward seal. This was estimated (by the ideal gas law) to pressurize the parachute compartment to 1.5psi above atmospheric pressure.

While unique, and weighing less than 100g, the system proved unreliable, and difficult to prepare, and reset.

IMG_20170425_192248+%281%29.jpg

Test Vehicle on the Pad

Test Vehicle on the Pad

2016 Design and flight performance

I lead my team to design a rocket air-frame from a variety of composite fabrics. The body tubes were built from Textreme 1015 carbon fiber fabric, The nosecone was made from 6K satin weave carbon fiber, and the main coupler and altimeter bay were made from aramid fabric.

The rocket used a high pressure CO2 parachute ejection system to control rocket apogee. At the TARC National competition, a CO2 leak corrupted our altimeter data resulting in a false apogee report from the competition assigned altimeter. Our higher performance onboard altimeter reported a less then 3’ difference between vehicle apogee and target apogee placing 40/700 in the launch, and second in presentation.

We also won the “Most Innovative Approach to Mission“ award, presented by Raytheon.

IMG_20170425_192343.jpg

Altitude Control System: CO2

I worked with a machinist to design a system to accept an 8g 800psi CO2 cartridge which was pre-punctured. This system used a bar and plunger to press a stack of o-rings to seal against the CO2 cartridge, the bar would slide into two grooves inside two bronze pylons. One of the pylons was attached to a small DC motor (not shown here) such that the motor could rotate the pylon, pushing the sealing bar out of the groove and allowing the CO2 to pressurize the parachute compartment.

This system proved to be incredibly reliable and was able to control the altitude of the rocket to within +/- 8’. This system flew on the 2015 and 2016 competition Rockets.


2015 design and Performance

Before I led the team, I worked as a member that primarily built the composite components of the rocket. The air-frame was made two layers of 3k twill weave carbon fiber, where the fins were made from 6 layers. This was the first year I advocated for the use of the Cesaroni F-79 motor that would later become the backbone of our competition strategy. Later in the year we began using the above mentioned CO2 ejection system.

The rocket and team performed exceptionally well, placing 34/700 and winning the “Best Rocket Craftsmanship“ award, presented by Lockheed Martin.

20140913_101832.jpg

2014 T-Con Competition

2014 T-Con Competition

2014 design and Performance

The records start getting thinner around here. The rocket flew on a Cesaroni F-59 re-loadable motor, and used a phenolic resin infused cardboard booster section and a lighter weight un-infused cardboard payload section.

This was the year I introduced the angled fin concept where the four fins were canted 7.5 degrees towards each-other. Canting the fins, increased drag on the booster section moving the center of pressure further aft-wards increasing the static margin of stability throughout the flight. This decreased wind-cocking and allowed for more consistent flights and better scores over all. This concept of designing a high-drag booster would be carried over for all subsequent years.

Placed 42/700 in the launch and did not compete in presentation.


IMG_20130511_125534.jpg

2013 Design and Performance

Not much has survived to the modern day, but I will include this year for the sake of completeness.

I designed the rocket, which utilized standard cardboard construction, birch wood fins, and a polypropylene nosecone. The rocket flew with a disposable casing EconoJet F-28. The rocket was durable, and definitely took a beating throughout the year. Against all odds we qualified for Nationals where we placed 92/700 in launch and did not compete in presentation